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Autor(en):

Medium: Fachartikel
Sprache(n): Englisch
Veröffentlicht in: Structural Engineering International, , n. 3, v. 3
Seite(n): 178-180
DOI: 10.2749/101686693780607840
Abstrakt:

Four elevated rail structures sequentially exhibited displacement-induced fatigue cracks between 1982 and 1991. Cost-effective retrofits were developed and implemented that have successfully controlled the problem. A case history of temporary and permanent retrofit solutions is presented. Through the use of instrumentation techniques, significant insight has been gained into fatigue cracking. A summary of the more-important findings of the programme, performed over a nine-year period, is also presented, along with recommendations for improving future designs.

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  • Reference-ID
    10003495
  • Veröffentlicht am:
    18.09.2002
  • Geändert am:
    28.10.2016
 
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